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- 2016 Dodge Charger Hellcat
I posted this up on my Facebook page but figure I'd post it here too for you guys who don't frequent the FB.
Finally, I found some time to work on an update. This won’t just be about my most recent failure, I’ll also go over previous ones too. Why would I openly talk about all this bad and potentially embarrassing stuff? Well, as per my usual self, I like to share and document what I can when I can and that includes my successes as well as my failures. I do it in hopes that it helps provide a fuller and more realistic picture of what to expect and what to prepare for should one try and take a similar journey. This is for the folks who have been waiting for me to post about any of it so if you’re curious about my recent motor mishaps, read on! Fair warning, it’s going to be long and somewhat technical, but I’ll try to keep it as simple as I can.
Here is what happened with each motor that I’ve had issues with over the last 6 months.
Up until late last year, I had been racing on a 441 Demon Performance / TKM built stroker motor for nearly 2 years. It was originally built in March 2021 where I picked it up in the middle of TX2K21 week, spent 40 straight hours getting it installed, slept for a couple hours, checked in for the event, and then spent time getting it tuned and ready to race. The engine did great and sounded insane! I was #1 qualifier with a blower only pass but then my transmission broke so that was that.
Over the next 20 months or so of racing on this motor, I went on to reset the Charger Hellcat quarter mile record multiple times with dozens of 7 second passes and a best 7.72 @ 178 with a 1.18 60’. The only real issue I had over this time span until the end was apparent cylinder pressure leakage. I had to chase this issue a few times which involved removing heads to send off for inspection, resurfaced, and head gaskets replaced. Besides that, all was well.
Then Oct/Nov of last year, I traveled to Maryland to try and hit 3 events spanning 4 weeks. The first event was MSHS Maryland 2022 and this motor continued to perform with no signs of trouble. I ran a pair of 7 second passes there, a 7.8 @ 180+ and 7.7 @ 183 in testing, had a couple major drivetrain failures but powered through and finished the race series with a Heavyweight class win. The next Maryland event was WCF Import vs Domestic where I made just one qualifier pass, was #2 after round 1 but developed a problem while on the return road that would prevent me from continuing to race. What happened there? The bolts holding my crank trigger reluctor wheel decided to back out, shear off after striking the back of the block, and then the wheel proceeded to cause all sorts of internal havoc as it loosely flopped around on the crank and grinded against the block. This was not a trackside repair job with the resources I had available, and a bit of material had unfortunately run through all the bearings so that was that and my trip ended with me heading to Demon Performance to swap in my freshly built back up motor. Just in time!
Before I go on to talk about my 2nd 441 stroker, one additional issue was found upon tear down for repair and refresh. One rod was slightly bent. The rods that were in it were Carillo Pro-H selected for being lighter in weight. This is important to note as I move on to the next motor to talk about. I was extremely happy with my 1st 441 motor and how it performed. Based on my experience with 441 #1, I wasn’t expecting any of the failures that occurred this year. Looking back, I made 27+ 7 second passes with it plus countless more 8 second passes over those 20 months. Interestingly, I didn’t start consistently trapping 180+ until I swapped to the new gen 5 Whipple 3.0L and 3.8L blowers with the new Nitrous Outlet intake plates and that’s when things started to become a bit more unreliable with the additional power I had at my disposal.
YouTube My Reluctor Wheel Fell Off
Finally, I found some time to work on an update. This won’t just be about my most recent failure, I’ll also go over previous ones too. Why would I openly talk about all this bad and potentially embarrassing stuff? Well, as per my usual self, I like to share and document what I can when I can and that includes my successes as well as my failures. I do it in hopes that it helps provide a fuller and more realistic picture of what to expect and what to prepare for should one try and take a similar journey. This is for the folks who have been waiting for me to post about any of it so if you’re curious about my recent motor mishaps, read on! Fair warning, it’s going to be long and somewhat technical, but I’ll try to keep it as simple as I can.
Here is what happened with each motor that I’ve had issues with over the last 6 months.
Up until late last year, I had been racing on a 441 Demon Performance / TKM built stroker motor for nearly 2 years. It was originally built in March 2021 where I picked it up in the middle of TX2K21 week, spent 40 straight hours getting it installed, slept for a couple hours, checked in for the event, and then spent time getting it tuned and ready to race. The engine did great and sounded insane! I was #1 qualifier with a blower only pass but then my transmission broke so that was that.
Over the next 20 months or so of racing on this motor, I went on to reset the Charger Hellcat quarter mile record multiple times with dozens of 7 second passes and a best 7.72 @ 178 with a 1.18 60’. The only real issue I had over this time span until the end was apparent cylinder pressure leakage. I had to chase this issue a few times which involved removing heads to send off for inspection, resurfaced, and head gaskets replaced. Besides that, all was well.
Then Oct/Nov of last year, I traveled to Maryland to try and hit 3 events spanning 4 weeks. The first event was MSHS Maryland 2022 and this motor continued to perform with no signs of trouble. I ran a pair of 7 second passes there, a 7.8 @ 180+ and 7.7 @ 183 in testing, had a couple major drivetrain failures but powered through and finished the race series with a Heavyweight class win. The next Maryland event was WCF Import vs Domestic where I made just one qualifier pass, was #2 after round 1 but developed a problem while on the return road that would prevent me from continuing to race. What happened there? The bolts holding my crank trigger reluctor wheel decided to back out, shear off after striking the back of the block, and then the wheel proceeded to cause all sorts of internal havoc as it loosely flopped around on the crank and grinded against the block. This was not a trackside repair job with the resources I had available, and a bit of material had unfortunately run through all the bearings so that was that and my trip ended with me heading to Demon Performance to swap in my freshly built back up motor. Just in time!
Before I go on to talk about my 2nd 441 stroker, one additional issue was found upon tear down for repair and refresh. One rod was slightly bent. The rods that were in it were Carillo Pro-H selected for being lighter in weight. This is important to note as I move on to the next motor to talk about. I was extremely happy with my 1st 441 motor and how it performed. Based on my experience with 441 #1, I wasn’t expecting any of the failures that occurred this year. Looking back, I made 27+ 7 second passes with it plus countless more 8 second passes over those 20 months. Interestingly, I didn’t start consistently trapping 180+ until I swapped to the new gen 5 Whipple 3.0L and 3.8L blowers with the new Nitrous Outlet intake plates and that’s when things started to become a bit more unreliable with the additional power I had at my disposal.
YouTube My Reluctor Wheel Fell Off
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